Automotive Forums .com - the leading automotive community online! Automotive Forums .com - the leading automotive community online!
Automotive Forums .com - the leading automotive community online! 
-
Latest | 0 Rplys

Stop Feeding Overpriced Junk to Your Dogs!

GET HEALTHY AFFORDABLE DOG FOOD
DEVELOPED BY THE AUTOMOTIVEFORUMS.COM FOUNDER & THE TOP AMERICAN BULLDOG BREEDER IN THE WORLD THROUGH DECADES OF EXPERIENCE. WE KNOW DOGS.
CONSUMED BY HUNDREDS OF GRAND FUTURE AMERICAN BULLDOGS FOR YEARS.
NOW AVAILABLE TO THE GENERAL PUBLIC FOR THE FIRST TIME
PROPER NUTRITION FOR ALL BREEDS & AGES
TRY GRAND FUTURE AIR DRIED BEEF DOG FOOD
Go Back   Automotive Forums .com Car Chat > Dodge > Neon | Plymouth Neon > 1st Gen 95-99
Register FAQ Community Arcade Calendar
Reply Show Printable Version Show Printable Version | Email this Page Email this Page | Subscription Subscribe to this Thread
 
Thread Tools
Old 09-29-2010, 08:24 PM   #1
tblake
In God We Trust
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Neon Compression test results, your diagnosis please????

So I posted here about headgaskets. The owner said 3 and 4 cylinders had low compression. Headgasket blown between?

http://www.automotiveforums.com/vbul....php?t=1049223

So then I found out that all cylinders have low compression. Starting on the timing belt side, compression goes 80psi, 60psi, 20psi, 0psi.

The car turns over fine, no knocks or ticks.

After finding this out I thought maybe the timing belt skipped. The car has 190k miles and I'm sure its the original belt. What else could cause compression readings like these?

A little background is the owners daughter was driving home and the car started losing power, she pulled over, turned it off, called for a ride (late at night), the next day the owner went back and tried to start it and got nothing. Turned over would not start. Upon me hearing it turn over, I know its turning WAY too fast as if it has no compression.

Today after work I started removing the side of the motor to check out the timing belt. Got up to the crank pulley, using a 3 jawed puller and I could not get it to budge, so I called it quits for the day.

First question is the compression results, what could cause readings this low besides the timing belt?

Second question, is this an interference motor? (2.0 16 valve the valve cover says)

Third question, anyone have any helpfull hints on getting the darn crank pulley off? And yes the bolt is loose, I'm not that dumb.
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 09-29-2010, 08:38 PM   #2
danielsatur
AF Enthusiast
 
Join Date: Mar 2008
Location: garner, North Carolina
Posts: 3,579
Thanks: 86
Thanked 100 Times in 100 Posts
Re: Neon Compression test results, your diagnosis please????

It sounds like a bad timing belt, a interference motor would bend valves and make noise.

I would set cylinder 1 @ tdc, and check timing marks.
If Timing is ok, it could be just burnt valves,or a bad head gasket.
danielsatur is offline   Reply With Quote
Old 09-29-2010, 08:57 PM   #3
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

Quote:
Originally Posted by danielsatur View Post
It sounds like a bad timing belt, a interference motor would bend valves and make noise.
Thats what I thought too, but knowing my luck, they are all bent, all 16. The way my luck goes, I could bend valves in a non interference GM 350 pushrod motor.

Quote:
Originally Posted by danielsatur View Post
I would set cylinder 1 @ tdc, and check timing marks.
If Timing is ok, it could be just burnt valves,or a bad head gasket.
That is exactly what I am going to do, but if the headgasket were blown, how could it cause low compression on all 4. I guess here again, its just my luck.
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 09-30-2010, 07:48 AM   #4
Oldsmobile Doctor
AF Regular
 
Join Date: Mar 2008
Location: Hilliard, Ohio
Posts: 203
Thanks: 0
Thanked 6 Times in 6 Posts
Re: Neon Compression test results, your diagnosis please????

Auto Zone has a tool # 27139 to remove the damper
Oldsmobile Doctor is offline   Reply With Quote
Old 09-30-2010, 09:50 AM   #5
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

Does it work and how much is it? There are no holes to screw into to use a regular dampner puller. I was just using a 3 jawed pulley puller and had no luck. Last one of these I put a timing belt in, I had the same issue. Dampner would not budge, I fought with it for a while and finally it went. Althought that time I was also just using the 3 jawwed puller.
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 09-30-2010, 10:45 AM   #6
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

Quote:
Originally Posted by Oldsmobile Doctor View Post
Auto Zone has a tool # 27139 to remove the damper
I looked it up and it looks excactly like the tool I am using.
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 10-01-2010, 07:13 AM   #7
Oldsmobile Doctor
AF Regular
 
Join Date: Mar 2008
Location: Hilliard, Ohio
Posts: 203
Thanks: 0
Thanked 6 Times in 6 Posts
Re: Neon Compression test results, your diagnosis please????

Look closer that one is special for Chrysler harmonic balancers. It comes with two pins that you put one or the other in the bolt hole depending on how deep the hole is.
Oldsmobile Doctor is offline   Reply With Quote
Old 10-02-2010, 02:21 AM   #8
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

I got it off.

Timing is dead on perfect, in fact the belt looks like its been changed in the past.

I began pulling the head off to see if the head gasket blew or if the head is cracked or if it has lower end issues.

Couple questions though.

What is that sensor in the lower battery tray? I started to take the tray out, I thought it was a nut holding the battery in and I spun nut around and ended up snapping the wires. No big deal but it looks to me like some sort of temperature sensor.

And if anyone has any pointers on getting some broken EGR valve bolts out. I'll probably soak it for a few days and try a vice grips. Or a little heat.

Also when the time comes I'll need some torque specs on the head bolts.

Thanks!!!
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 10-02-2010, 08:20 AM   #9
Oldsmobile Doctor
AF Regular
 
Join Date: Mar 2008
Location: Hilliard, Ohio
Posts: 203
Thanks: 0
Thanked 6 Times in 6 Posts
Re: Neon Compression test results, your diagnosis please????

1st Tighten to 25 ft. lbs.
2nd Tighten to 50 ft. lbs.
3rd Tighten to 50 ft. lbs
4th Tighten an additional ¼ turn
(DO Not use a torque wrench for 4th step)
Oldsmobile Doctor is offline   Reply With Quote
Old 10-05-2010, 08:59 PM   #10
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

Got the head off, piston 4 has a chip missing (hence the 0psi compression) and all 4 cylinders seem to have some scoring. Motor is toast. Looks like the car is going to get parted out and hauled to the junkyard.

If anyone needs any parts, shoot me a PM or an email. I'd rather not ship heavy things like the head or transmission (which was acting up towards the end I'm also told). But I have no problem shipping the smaller stuff it you cover the actual shipping charges and add a little extra for paypal fees.

More details on craigslist.

http://minneapolis.craigslist.org/hn...991101037.html





__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
Old 10-06-2010, 10:53 AM   #11
danielsatur
AF Enthusiast
 
Join Date: Mar 2008
Location: garner, North Carolina
Posts: 3,579
Thanks: 86
Thanked 100 Times in 100 Posts
Re: Neon Compression test results, your diagnosis please????

What's the year and condition of car, other than a bad motor?
I gave my 95TC away, it had a bad engine and still have regreats.

* Pistons & rings on a 4-cylinder is 50% cheaper than a V8.
danielsatur is offline   Reply With Quote
Old 10-07-2010, 10:19 AM   #12
tblake
In God We Trust
Thread starter
 
tblake's Avatar
 
Join Date: Nov 2003
Location: Maple Lake, Minnesota
Posts: 5,971
Thanks: 4
Thanked 24 Times in 23 Posts
Send a message via MSN to tblake
Re: Neon Compression test results, your diagnosis please????

its a 95, a little over 160,000 miles if I remember right, the windshield is cracked, paint baked off the roof, back corners of the body are rusted out, front bumper cover is cracked.

It was a 500.00 car 2 years ago.
__________________
-2000 Grand Prix GTP 170,000mi (daily driver)
-2000 Olds Alero 100,000mi (soon to be DD with gas at $3.45/gal)
-1997 Chev K1500 4x4 115,000mi (Natalie's truck [nans_grandprix])


AF "2.0" Community Guidelines

Conservative Victory 2012!!!

"I'll Keep my Guns, Freedom, and Money. You can Keep the Change!"

----->>>>> Did You Know? <<<<<-----
tblake is offline   Reply With Quote
 
Similar Threads
Thread Thread Starter Forum Replies Last Post
compression test results good or bad?? B16Civic93 Let's get Technical! 2 05-13-2004 05:20 PM
Cylinder Compression Test Results.....need some help johnneyinteg Wrangler 2 02-13-2004 08:56 PM
Cylinder Compression Test Results....need some help johnneyinteg Engineering/Technical 2 02-13-2004 10:48 AM
Compression test results after almosrt 2yrs of N20 whtteg Forced Induction 21 05-23-2003 03:11 PM
compression test results on D16a6 RedRacerCivic '88 - '91 Civic | CRX | Wagon | Shuttlee 2 05-22-2003 02:57 AM

Reply

POST REPLY TO THIS THREAD

Go Back   Automotive Forums .com Car Chat > Dodge > Neon | Plymouth Neon > 1st Gen 95-99


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off



All times are GMT -5. The time now is 12:04 PM.

Community Participation Guidelines | How to use your User Control Panel

Powered by: vBulletin | Copyright Jelsoft Enterprises Ltd.
 
 
no new posts