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95 neon no accellerationtrifit1 11-30-2005, 11:42 AM My daughters SOHC sat for a month. After that it does not have any pick up as it did before, this what I have done: 1. Checked air intake 2. checked fuel pressure and injectors 3. changed coilpack ,plugs and wires 4. checked exhaust for resriction 5. It starts and idles/revs normal without load 6. recently changed VSS, CPS, Cam pos sens 7. No codes now, got an 11 at first. 8. compression 160-175psi 9. cant see or hear any vacuum leaks 10. put in new gas and injector cleaner Any suggestions? sound familliar to anyone? das2123 11-30-2005, 06:38 PM Could be water in the gas tank, bad or going bad EGR valve. You say you got a code 11, have you checked the compression since then? trifit1 11-30-2005, 08:47 PM When it first happened it died on me a couple of times and would not start until the next day. I did not check if it was fuel or spark related. I pulled the fuel pump fuse to clear the codes. Has not thrown another code since and starts right up. When I step on the gas it just seems to bog down and slowly picks up speed. Like its plling a heavy load. Will not rev up and ATX does not downshift. Basically like running on 1/2 power, das2123 12-01-2005, 08:20 AM Out of curiosity, what kind of spark plugs did you put in there? Your compression is a little low also. trifit1 12-01-2005, 09:48 AM I changed them out with Bosch platiums, I was going to try putting the old but still good NGK's ' I heard that neons dont do well with platinum plugs. The compression thing has not changed since the power loss so I don't think they are related. das2123 12-01-2005, 10:34 AM I changed them out with Bosch platiums, I was going to try putting the old but still good NGK's ' I heard that neons dont do well with platinum plugs. The compression thing has not changed since the power loss so I don't think they are related.You heard right...put some stock champion coppers in there and that should help you out. The platinum plug does not work well in the neon. trifit1 12-01-2005, 04:52 PM Well, the plug change made a big difference, but when I step on it the ATX does not downshift to accelerate, the car pulls well up to speed though. When I manually hit D1 the thing doesn't go at all. Maybe a clogged filter or band adjustment needed? das2123 12-01-2005, 05:19 PM Well, the plug change made a big difference, but when I step on it the ATX does not downshift to accelerate, the car pulls well up to speed though. When I manually hit D1 the thing doesn't go at all. Maybe a clogged filter or band adjustment needed?First off, don't manually shift an ATX neon, bad idea. You may need a reverse band adjustment and check your fluid level. trifit1 12-01-2005, 09:16 PM Thanks for the help, it's a load off to have it running strong again. Will get into the trans tomorrow 1thunder 12-01-2005, 09:57 PM check the kickdown linkage may be siezed it's located under battery tray it should move back and forth freely trifit1 12-01-2005, 10:02 PM that would make sense as it sat idle outside for a month in some really wet weather trifit1 12-02-2005, 05:36 PM Is that what Haynes calls the throttle pressure cable? It appears to be out of adjustment, the cable end is hanging out of it's connection on the throttle body vBulletin®, Copyright ©2009, Jelsoft Enterprises Ltd.
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